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The car had the original block and heads and looked like it had never been taken apart. The intake, carburetor and exhaust manifolds had been replaced, so I went to many swap meets to find some correctly date coded replacements. The transmission had also been replaced with a TH350. I found a Muncie M20, which is not correct for the car, but it seemed like a better solution than a Saginaw. I'm still trying to figure out how to route the speedo cable though. |
The motor is basically stock with just a few internal modifications, such as;
Cylinders bored .030 over.
High volume oil pump.
Hardened valves and valve seats.
Polished exhaust chambers. Intake chambers were left rough to better vaporize the fuel.
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This was the starting point. It hardly needed a thing ; -) |
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The motor comes out for a complete rebuild. |
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The motor slowly starts to go back together. |
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Three years later it's almost complete and ready to go back in. |
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A milestone is reached as the motor finds it's way back into the car. |
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It's very tempting to try to start it, but that will have to wait for another day. |
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